The Robinson hot air engine was common in
England. Patented in 1889, large quantites of them were produced as
recently as the 1920s. Used in England and Europe until the WW-II era,
they were displaced by electric motors and small but powerful
internal combusion engines.
The Robinson's displacer moves vertically and the power piston moves horizontally. This 90° arrangement makes for a very compact size. In fact, the power piston connecting rod weaves its way through the displacer linkage. I've long been intrigued with this style of engine and hoped to buy or build one, some day. Then, in 2004 my friend Carl Carlson made my dream come true. He helped me buy a modest collection of hot air engines, including a quarter-scale Robinson.
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As you can see in Carl's picture, the little rascal looks really cute. But, upon getting it home, it refused to run. This didn't come as any great surprise. That happens. So, I undertook an overhaul, but, as it turned out, it became a complete re-build. I hope you like how it turned out.
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After I stripped off the old paint, I discovered the base had
been broken in three pieces and had been brazed,
arc welded, and J-B Welded, none of them being very pretty.
It took a lot of JB-Welding, filing and sanding to hide the
repairs.
You can see the new graphite piston, new crank disk, crank pin and the new cold water inlet. I also sandwiched in as much high temperature gasket material as bolt length would allow to help make a better thermal barrier between the base and mid-section. Because of the high temperature from the fire, underneath, that makes it run, the base is painted with stove paint. Seeing as how the mechanism requires oil, and flat paint looks ugly when it gets oil on it, the top is glossy. |
So, I started searching through my pictures of full-scale Robinsons and I finally found the answer. One, and only one, picture showed an external coolant tank connected. Time for a re-design! |
Here are some of the parts I replaced. The cylinder in the picture
is the displacer. This one had suffered some major abuse during
construction. Part of the brass had been melted away!
The subsequent lead solder repairs made it so heavy it was better
to start all over and build another, much lighter, out of aluminum.
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The 3/16-inch copper tubing was supposed to be the boundary between the cooling water and the working air (but it leaked). Being glued in place, the only way to get it out was to gently hammer the parts apart and shear it in two. It got replaced with a Teflon-packed seal that withdraws easily whenever disassembly is required. |
All in all the Robinson has been a very fun project. It now runs merrily for hours on end, non-stop. Right now the little rascal stands at the top of my "Favorite" list. I hope you liked it, too. |
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